I spent a little time this morning running the headlight wires as well as 2 wires for future turn signals.
I had went to NAPA and picked up a new dimmer switch, but when I got it home it did not mount correctly so I boxed it back up and it will be returned. I tested the old switch and it appeared to be working properly so I added a jumper wire to the broken spade connection so I could use the middle pin.
Then I replaced the alternator wire with a new one and made it neat. I also purchased a new starter to solenoid cable but have not hooked it up yet.
Man I need to do something with that bracket! |
Cleaned up the inside a bit so I will be ready to go at it this weekend and hopefully get the truck back on the ground.
I got tired of putting knots on my head from the running board bracket so I covered it with a sock and shop gloves LOL Ouch!
Tonight I decided to build the 12 to 6 volt reducer. It came out nice and it works! I used an old heat sink ( aluminum base everything is mounted to) from a broken PC power supply. This should put out about 10 amps and that should be plenty to run the wiper motor and gauges.
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